Probably in the process of abandoning the old wellbore.
That's what I'm thinking.
Great info Doug. Tell Bob I said hi.
BlackBrush has not completed the North lateral...Beth, I will pass the message, thanks!
03/06/2018 | 05 | 18213 | 3/2/18, SET KICK OFF PLUG @ 13,980'. 3/4/18, KICKING OFF CEMENT PLUG. 3/6/18, CURRENT OPERATIONS, TIH W/CEMENT RETAINER. |
Sorry, once I copied the above, I couldn't put a comment. So, this is the latest that was posted today on Serial number 250723.
How about it Rockman, Skip or Jay, or one of you people that is much smarter than me.
1. vb. [Drilling]
To drill a secondary wellbore away from an original wellbore. A sidetracking operation may be done intentionally or may occur accidentally. Intentional sidetracks might bypass an unusable section of the original wellbore or explore a geologic feature nearby. In the bypass case, the secondary wellbore is usually drilled substantially parallel to the original well, which may be inaccessible due to an irretrievable fish, junk in the hole, or a collapsed wellbore.
|
250723 | BBJB PROPERTIES LLC | 001 | W4983 | 2593 | 40 | 00 | 023 | 01N | 02E | 01/19/2018 | 17079204600000 |
PRMT DATE | SPUD DATE | STAT DATE | ST CD |
---|---|---|---|
01/19/2018 | 01/19/2018 | 01 |
WELL SURFACE COORDINATES
Surface Longitude | Surface Latitude | Lambert X | Lambert Y | Ground Elevation | Zone | Datum |
---|---|---|---|---|---|---|
92-14-50.6 | 31-2-32.36 | 2079120 | 136739 | 52.4 | N | NAD-27 |
WELL SURFACE COORDINATES GENERATED BY DNR
UTMX 83 | UTMY 83 | LONGITUDE 83 | LATITUDE 83 |
---|---|---|---|
571805.44200136 | 3434556.55598091 | -92.24751942 | 31.04251245 |
BOTTOM HOLE COORD
EFFECTIVE DATE | END DATE | PLUGBACK TOTAL DEPTH | TRUE VERTICAL DEPTH | MEASURED DEPTH | LAT DEG | LAT MIN | LAT SEC | LONG DEG | LONG MIN | LONG SEC | COORDINATE SOURCE | LAMBERT X | LAMBERT Y | ZONE | COORDINATE SYSTEM |
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
01/19/2018 | 14500 | 18206 | 31 | 1 | 54.07 | 92 | 14 | 49.02 | 02 | 2079267 | 132871 | N | 01 | ||
01/19/2018 | 14500 | 18206 | 31 | 1 | 54.738 | 92 | 14 | 49.486 | 02 | 3360058 | 193574 | N | 02 | ||
01/19/2018 | 14500 | 18206 | 31 | 2 | 59.83 | 92 | 14 | 49.99 | 02 | 2079167 | 139514 | N | 01 | ||
01/19/2018 | 14500 | 18206 | 31 | 3 | .491 | 92 | 14 | 50.46 | 02 | 3359958 | 200217 | N | 02 |
WELL HISTORY
SERIAL | WELL NAME | WELL NUM | ORG ID | FIELD | ST CD | PT | WELL CLASS | EFF DATE | END DATE | STAT DATE |
---|---|---|---|---|---|---|---|---|---|---|
250723 | BBJB PROPERTIES LLC | 001 | W4983 | 2593 | 01 | 00 | 01/19/2018 | 01/19/2018 |
SCOUT INFO
REPORT DATE | WELL STATUS | MEASURED DEPTH | TRUE VERT DEPTH | DETAIL |
---|---|---|---|---|
03/14/2018 | 05 | 3/12/18, FUNCTION TESTED BOP'S. 3/13/18, SLIDE AND ROTATE DRILLING @ 13,898' | ||
03/06/2018 | 05 | 18213 | 3/2/18, SET KICK OFF PLUG @ 13,980'. 3/4/18, KICKING OFF CEMENT PLUG. 3/6/18, CURRENT OPERATIONS, TIH W/CEMENT RETAINER. | |
02/27/2018 | 05 | 2/25/18, REACHED TD OF 18,213' 2/27/18, DP STUCK @ 14,228', PRESENT OPERATIONS, RIH W/STRING SHOT FOR ATTEMPTED BO @13,014' | ||
02/20/2018 | 05 | 2/20/18, TRIPPING IN HOLE WITH MUD MOTOR AND BIT FOR AN ATTEMPT TO ENTER SOUTHERN LATERAL, TD 13,107'. | ||
02/14/2018 | 05 | 2/9/18, TESTED HYDRILL & NOV TYPE 6012 10 M PIPE RAMS 250 PSI LOW, 5000 PSI HIGH FOR 30 MINS. TEST OK. 2/13/18, PRESENT OPERATIONS, GOING INTO HOLE, CIRCULATE & CONDITION OLD MUD AND DRILLING AS NECESSARY @ 7300' | ||
02/07/2018 | 05 | 2/6/2018, PRESENT OPERATIONS, WASHING & REAMING @4000' | ||
01/30/2018 | 05 | 3991 | PRESENT OPERATIONS: FISHING FOR JUNK @ 3991' | |
01/24/2018 | 05 | 1/23/18, RE-ENTERED 1/23/18, TESTED HYDRILL & NOV TYPE 6012 10M PIPE RAMS TO 250 PSI LOW & 5000 PSI HIGH FOR 30 MINS. ON CHART, TEST OK. 1/24/18, PRESENT OPERATIONS, WASHING DOWN. | ||
01/19/2018 | 01 | 18206 | N 8 D 1' W-31,040.9' FR NGS MONU."FARR AZ MK" IN SEC 23.PBHL #1: N 57' 43" E-2775.69' FROM SL IN SEC 23.PBHL #2:S 2 D 10' 26" E-3871' FR SL IN SEC 23. (REDRILL OF SN 220356). |
PERFORATIONS
SERIAL NUM | COMPLETION DATE | UPPER PERF | LOWER PERF | SANDS | RESERVOIR |
---|
WELL TESTS
RPT TYP | TEST DATE | RPT DATE | OIL POT | COND | GAS DEL | WATER | BSW% | FLOW PRES | SHUTIN PRES | CHOKE | UPPER PERF | LOWER PERF | BOT HOLE PRES |
---|
WELL ALLOWABLES
EFFECTIVE DATE | END DATE | LUW CODE | LUW TYPE CODE | ALLOWABLE | ESTIMATED POTENTIAL | CURRENT ALLOWABLE TYPE |
---|
LEASE\UNIT\WELL PRODUCTION
RPT DATE | LUW CODE | STORAGE FAC | DOC USE | WELL CNT | OPENING STK | OIL PROD(BBL) | GAS PROD(MCF) | DISPOSITION | CLOSING STK | PARISH |
---|
CASING
COMPLETION DATE | CASING SIZE | WELLBORE SIZE | CASING WEIGHT | UPPER SET DEPTH | LOWER SET DEPTH | CEMENT SACKS | TEST PRESSURE | HOURS UNDER PRESSURE | TEST DATE | CASING PULLED | CREATION PROCESS |
---|
PLUG AND ABANDON
P and A DATE | LOCATION TYPE | CASING CUT TYPE | CASING CUT DEPTH | MUD WEIGHT LEFT | COMMENTS |
---|
PLUGS
PLUG TYPE | UPPER PLUG DEPTH | LOWER PLUG DEPTH | SACKS OF CEMENT | SLURRY WEIGHT |
---|
TUBING AND PACKERS
COMPLETION DATE | TUBING SIZE | TUBING LOWER DEPTH | TUBING UPPER DEPTH | PACKER DEPTH |
---|
WORK PERMITS
REFERENCE NUMBER | APPLICATION DATE | EXPIRATION DATE | WORK PERMIT TYPE | WORK PERMIT STATUS | WORK PERMIT STATUS_DATE | TOTAL DEPTH | WORK_PERFORMED | DOCUMENTATION RECEIPT DATE | TEST SAND | WORK DESCRIPTION |
---|---|---|---|---|---|---|---|---|---|---|
44-18 | 02/01/2018 | 02/01/2019 | SIDETRACK NEW BHL (EXISTING WELL) | VERBAL | 03/07/2018 | 18000 | N | AUSTIN CHALK | DRILL PIPE STUCK. BK OFF DP @ 14,120'. PUMP 38 BBL OF 17 PPG CMT AND SPOT BAL PLUG. CMT FROM 13,980' TO 13,033'. CMT 150' INSIDE 7-5/8". KOP 13,300. DRILL NEW LAT 250'E OF EXISTING LAT TO TD 18,000 | |
48-18 | 03/06/2018 | 03/06/2019 | SIDETRACK NEW BHL (EXISTING WELL) | VERBAL | 03/07/2018 | 18000 | N | AUSTIN CHALK | WP 44-18 UNSUCCESSFUL: SET CMT RETAINER @ 13,089 & PUMP 100 BBLS CMT FROM 13,089 TO 13,511'. PUMP 3 BBLS CMT ON TOP OF CMT RETAINER. SET WHIP STOCK AT 13,083 AND DRILL NEW LAT TO 18,000. |
Shale drilling and lithium extraction are seemingly distinct activities, but there is a growing connection between the two as the world moves towards cleaner energy solutions. While shale drilling primarily targets…
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AboutAs exciting as this is, we know that we have a responsibility to do this thing correctly. After all, we want the farm to remain a place where the family can gather for another 80 years and beyond. This site was born out of these desires. Before we started this site, googling "shale' brought up little information. Certainly nothing that was useful as we negotiated a lease. Read More |
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