Anybody know what happend in this unit? we have not heard or received anything in a year .did they shut?

Views: 53

Reply to This

Replies to This Discussion

The well is listed as producing, status code 10.  There are fifteen months of production shown through 10/31/2010 totaling 171.095 MMcfd (million cubic feet per day).  There are other sub-economic wells in this area of the Logansport Field.  Depending on your decimal interest in the unit, you may only receive a check once a quarter or twice a year.

OH, here is the initial test results.

 

Chesapeake, Blackstone 20 #H1 Well, Serial #239478, S20(20/29)-T11N-R15W, DeSoto Parish, 1214 Mcfd, 26/64" Choke, 2018 psi Flowing Pressure

RSS

Support GoHaynesvilleShale.com

Blog Posts

History of GoHaynesvilleShale

The History of GoHaynesvilleShale.com

GoHaynesvilleShale.com (GHS) was launched in 2008 during a pivotal moment in the energy industry, when the Haynesville Shale formation—a massive natural gas reserve lying beneath parts of northwest Louisiana, east Texas, and southwest Arkansas—was beginning to attract national attention. The website was the brainchild of Keith Mauck, a landowner and entrepreneur who recognized a pressing need: landowners in the region had little access to…

Continue

Posted by Keith Mauck (Site Publisher) on May 21, 2025 at 6:00

Not a member? Get our email.

Groups



© 2025   Created by Keith Mauck (Site Publisher).   Powered by

Badges  |  Report an Issue  |  Terms of Service