Just wondering why the production for BSI/USFS Unit F6, lower for the month of April, 2015?
According to RRC report:
1/2015 -296,547
2/2015 -310,191
3/2015 -213,640
4/2015 -2,952
5/2015 -295,943
Didn't see a report for 6/2015 yet reported, but was wondering if this is all that will be reported for April, or if not, what happened?
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June won't be reported until Aug 1. XTO is pretty good about reporting on the 1st. F11 (same pad) had a casing leak which they had to do a cement squeeze on to fix it. Both wells had to be shut down while all that was going on (safety). F11 only reported 2082 mcf in April.
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In researching the decades-old Tuscaloosa Trend and the immense wealth it has generated for many, I find it deeply troubling that this resource-rich formation runs directly beneath one of the poorest communities in North Baton Rouge—near…
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