Just wondering why the production for BSI/USFS Unit F6, lower for the month of April, 2015?
According to RRC report:
1/2015 -296,547
2/2015 -310,191
3/2015 -213,640
4/2015 -2,952
5/2015 -295,943
Didn't see a report for 6/2015 yet reported, but was wondering if this is all that will be reported for April, or if not, what happened?
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June won't be reported until Aug 1. XTO is pretty good about reporting on the 1st. F11 (same pad) had a casing leak which they had to do a cement squeeze on to fix it. Both wells had to be shut down while all that was going on (safety). F11 only reported 2082 mcf in April.
Shale drilling and lithium extraction are seemingly distinct activities, but there is a growing connection between the two as the world moves towards cleaner energy solutions. While shale drilling primarily targets…
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