Samson Lone Star / Stacy Gas Unit 1- Well 5-H / IP of 8.453 mcfd in Waskon-Haynseville

From E. Texas Drilling Report / Jan 2 2010:

Samson Lone Star completed the Stacy Gas Unit 1 Well No. 5H to 15,741 feet, 5.5 miles northwest of Waskom in the Waskom Field. On a 22/64-inch choke the well potentialed 8.453 million cubic feet of natural gas in the Haynesville formation.

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Harrison County

Penn Virginia Oil & Gas completed the Devon Gas Unit Well No. 6 to 10,560 feet, in a lease 7.1 miles northwest of Marshall in the Southwest Woodlawn Field. The well potentialed 501,000 cubic feet of gas on a 48/64-inch choke in the Cotton Valley.


Samson Lone Star completed the Stacy Gas Unit 1 Well No. 5H to 15,741 feet, 5.5 miles northwest of Waskom in the Waskom Field. On a 22/64-inch choke the well potentialed 8.453 million cubic feet of natural gas in the Haynesville formation.


Tony W. Clemons completed the Davis Frank Estate Gas Unit Well No. 3 to 6,950 feet, 5.8 miles north of Marshall in the Woodlawn Field and it potentialed 1.220 million cubic feet of gas. Choke size is unknown. Production is in the Pettit Page.

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