Looks like there has been a new Permit issued for Crowell well SW of Glenmora.   Was SN# 251311 & now it is SN# 251809.

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Interesting news on sonris concerning Crowell lm30h number 251809 -a permit dated 09/16/2020 to perforate/return to production has been approved

Results of that work will be interesting to see. Thanks for posting

Can’t wait to see what happens there. 

Its good news with glimmer of hope,.,, but is it economical at $40/oil and $2/gas?

If I remember correctly, there were massive volumes of water being produced daily here. Operating costs to handle this water will be high. An SWD is the only way to even think about producing this well - and that up front capital cost puts a big hit on economics.

Skip - has SONRIS posted info on the SWD's that were drilled in this area (assumingly for this well).?

The Crowell SWD well was permitted June 9 but has not been reported as drilled.  Of the three SWD wells listed below only the first, BENTLEY-GLENMORA 31 SWD, is operational.  The second SWD well, BENTLEY-GLENMORA 25 SWD, is not reported as drilled also.

http://sonlite.dnr.state.la.us/sundown/cart_prod/cart_con_wellinfo2...

 

S5683

SOUTHWIND OIL & GAS LLC

 

Cnt

Well Serial

Well Name

Well Num

Status

Class

Class Type

API Number

Org ID

Field ID

Permit Date

Sec-Town-Rng

Parish

LUW Association

1

251311

CROWELL LM 30

001

18

17079205460000

S5683

6565

28-SEP-18

030-01S-01W

40

GO TO LUW INFO

16005

2

251809

AUS C RA SU80;CROWELL LM 30 H

002

18

17079205470000

S5683

6565

27-JUN-19

030-01S-01W

40

GO TO LUW INFO

23590

3

252119

AUS C RA SUX;CROWELL LM 3 H

001

18

17079205500000

S5683

2595

26-NOV-19

003-01S-01W

40

GO TO LUW INFO

23010

4

975517

BENTLEY-GLENMORA 31 SWD

001

09

II

5

17079880700000

S5683

6565

28-NOV-18

031-01S-01W

40

GO TO LUW INFO

5

975679

BENTLEY-GLENMORA 25 SWD

001

02

II

5

17079880710000

S5683

6565

15-JAN-20

025-1S-2W

40

GO TO LUW INFO

6

975704

CROWELL LM 3 SWD

001

02

II

5

17079880720000

S5683

2595

09-JUN-20

003-01S-01W

40

GO TO LUW INFO

yes , lots of water... like 13k barrels/ month.

Any new input on how this well is doing?

The well restarted reporting monthly production in January.

LEASE\UNIT\WELL PRODUCTION

RPT DATE

LUW CODE

STORAGE FAC

DOC USE

WELL CNT

OPENING STK

OIL PROD(BBL)

GAS PROD(MCF)

DISPOSITION

CLOSING STK

PARISH

03/01/2022

052211

1

542

11480

84348

11568

454

RAPIDES

02/01/2022

052211

1

809

13637

89974

13904

542

RAPIDES

01/01/2022

052211

1

0

11196

67837

10387

809

RAPIDES

05/01/2020

052211

1

1170

9999

66466

9820

1349

RAPIDES

04/01/2020

052211

1

1554

22770

163043

23154

1170

RAPIDES

03/01/2020

052211

1

1675

29718

212851

29839

1554

RAPIDES

02/01/2020

052211

1

1523

27947

202968

27795

1675

RAPIDES

01/01/2020

052211

1

0

6004

47298

4481

1523

RAPIDES

Back on production but still making MASSIVE water volumes. January 2022 was 6100 BWPD / Late March 2022 rate was up to 7880 BWPD. Oil and gas rates dropping over that time as are pressures. Looks like they had to open up the choke on this well to keep if flowing.

I'd watch this well over the next year - don't be surprised if it is shut down again due to economics and lower O&G volumes.

Figure operator opened it back up in January 2022 to take advantage of O&G prices.

RPT TYP TEST DATE RPT DATE OIL POT COND GAS DEL WATER BSW% FLOW PRES SHUTIN PRES CHOKE UPPER PERF LOWER PERF BOT HOLE PRES
DM-1R 03/30/2022 05/01/2022 350 2650 7880 96 4255 33/64 16157 22372
SDM2O 01/31/2022 01/31/2022 685 4250 6810 84 7900 23 16157 22372
DM-1R 03/24/2020 05/01/2020 937 13099.4 93.3 6429 39/64 16157 22372
SDM2O 03/24/2020 03/24/2020 1007 7083 13127 93 6433 39 16157 22372

Item copied fine from SONRIS but gets distorted once "saved" on this site / cannot fix it.

Top two lines are the critical info

3/30/22 test date / reported 5/1/22

Potential 350 BO, 2650 MCF & 7880 BW per day

4255# flowing pressure on 33/64" choke

Earlier test

1/31/22 test date / 1/31/22 report date

Potential 685 BO, 4250 MCF & 6810 BW per day

7900# flowing pressure on 23/64" choke

Higer rates and pressures after being shut in for extensive period was to be expected. But things dropping quickly.

Decent royalty checks but operator watching their margins very closely here as water goes up and O&G go down. Lease operating expenses - even with SWD well - are probably high. Imagine handling and injecting close to 8000 BW per day (quarter million BW per month). May need another SWD here in time

Doesn't look too good for this Rapides Parish area or maybe just this well.  It's been said this area has alot of water and pressure.

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