Yes, that Continental Resources.  Partial sections 17-20, 3N - 11W.  Just east of the South Toledo Bend State Park, Toro Road area.

https://ucmwww.dnr.state.la.us/ucmsearch/UCMRedir.aspx?url=http%3a%...

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Suggest that members do a little Google search for Continental Resources.  Hint: Big Bakken oil field player.

If anyone has a way to contact Kirk Barrell, they should let him know so he can post his thoughts on this new AC player.  Continental is a large publicly traded company that has never focused on the Chalk or even Louisiana so this is very interesting.

I agree that it would be good to hear Kirk's opinion but don't you think he already knows about this application?  If not, he must be solely focused on solar farms these days.

Assuming that Continental will be chasing Austin Chalk here with a horizontal / frac stimulation effort.

Note the well noted on SE part of the plat (Swift Sonat horizontal). Drilled and "completed" in 1992. Swift got the lateral to TD (about a 4000' lateral in the AC) after having to abandon original lateral. At TD, Sonal took over operations .

A frac was attempted on the lateral (in slotted liner). Well only IP'd 50 BO & 270 MCF per day from the entire lateral. Well only produced about 900 BO before being abandoned. This was called North Haddens Field.

I attached the hand written scout card for this well. No idea what this cost but it was a LOT.

For their sake, I hope that Continental has some good data to support this effort - not a lot of well control here to support AC matrix porosity play.

Attachments:

On 12/10,  Nabors Drilling Rig #B15 reported 10 days Drilling Ahead @ 9776' on the Continental Resources Labokay 20-17 H #1.

Can anyone explain what all of this means? I was able to find it on Sonris, but I don't understand it except it looks like they now have a permit to frac. Thanks.

Review Well Information

WELLS

SERIAL WELL NAME WELL NUM ORG ID FIELD PARISH PROD TYPE SEC TWN RGE EFFECTIVE DATE API NUM
253085 AUS C RA SUB;LABOKAY 20-17 H 001 C111 4382 58 00 020 03N 11W 11/12/2021 17115202380000
PRMT DATE SPUD DATE STAT DATE ST CD
11/12/2021 11/12/2021 01

WELL SURFACE COORDINATES

Surface Longitude Surface Latitude Lambert X Lambert Y Ground Elevation Zone Datum
0-0-0 0-0-0 1682838 202356 317 N NAD-27

WELL SURFACE COORDINATES GENERATED BY DNR

UTMX 83 UTMY 83 LONGITUDE 83 LATITUDE 83
450973.95771582 3453995.45960134 -93.51472795 31.21908019 View GIS

BOTTOM HOLE COORD

EFFECTIVE DATE END DATE PLUGBACK TOTAL DEPTH TRUE VERTICAL DEPTH MEASURED DEPTH LAT DEG LAT MIN LAT SEC LONG DEG LONG MIN LONG SEC COORDINATE SOURCE LAMBERT X LAMBERT Y ZONE COORDINATE SYSTEM
11/12/2021 9632 20318 02 1682699 212632 N 01

WELL HISTORY

SERIAL WELL NAME WELL NUM ORG ID FIELD ST CD PT WELL CLASS EFF DATE END DATE STAT DATE
253085 AUS C RA SUB;LABOKAY 20-17 H 001 C111 4382 01 00 11/12/2021 11/12/2021

SCOUT INFO

REPORT DATE WELL STATUS MEASURED DEPTH TRUE VERT DEPTH DETAIL
01/10/2022 31 20125 9712 SCOUT CODE 31: 1/4/2022 TUES. 6:00 AM - RUN 5'',18#, P-110, WEDGE 513 CASING F/ 6650' T/ 10,322'. SWAP T/ 5 1/2'' HANDLING EQ RUN CSG T/ 13,750'; 1/5/2022 WED. 6:00 AM - RUN 5 1/2" CSG F/ 13,750' T/ 16,959' WASH & REAM TO BOTTOM. LAND HANGER WITH SHOE @ 20,125'. CIRC 1.5 CSG CAPACITIES, CEMENT AS PER PLAN WITH FULL RETURNS. BUMPED PLUG W/ 3500 PSI. BLED BACK 5 BBLS. FLOATS HELD OK R/D CEMENTERS AND BACK OUT LANDINGJT; 1/6/2022 THURS. 6:00 AM - SET PACK OFF, CLEAN PITS,FLUSH SURFACE LINES, ND BOPS, NU TBG HEAD, TEST SEALS TO 15K VOID TO 10K. LD 60 STANDS DP FROM DERRICK. START RIGGING DOWN TOP DRIVE.; 1/7/2022 FRI. 6:00 AM - FINISH CLEANING PITS RIG RELEASE 11:00HRS, 1/6/22. RIG DOWN AND WASH RIG; 1/8/2022 SAT. 6:00 AM - RIG DOWN ON LABOKAY 20-17 H1, SCATTER AND WASH RIG.; 1/9/2022 SUN. 6:00 AM - RIG DOWN ON LABOKAY 20-17 H1, SCATTER AND WASH RIG; 1/10/2022 MON. 6:00 AM - WASH RIG AND CLEAN CELLAR
01/03/2022 31 20125 9712 SCOUT CODE 31: 12/28/2021 TUES. 6:00 AM - TIME DRILL AS PER PLAN F/ 16,431' T/ 16,438' DRILL 6 3/4" LATERAL T/ 16,713. CONFIRM NOT IN OLD HOLE. CBU. TOOH TO BHA.; 12/29/2021 WED. 6:00 AM - LD SIDE TRACK ASSY, FUNCTIONED BOP'S, PU LATERAL ASSY, TIH CUT DRILL LINE @ 7,100'. TIH & RELOG LAST 30' TO BOTTOM; 12/30/2021 THURS. 6:00 AM - DRILL 6 3/4" LATERAL F/ 16,713' T/ 18,208' AT 18,038' (TD ORIGINAL WELLBORE) WAS 49' FROM OLD WELL.; 12/31/2021 FRI. 6:00 AM - DRILL 6 3/4" LATERAL F/ 18,208' T/ 19,100' ; 1/1/2022 SAT. 6:00 AM - DRILL 6 3/4" LATERAL F/ 19,100' T/ 20,135' ( TD ). PUMPED 40 BBL SWEEP AND CIRC. CLEAN UP CYCLE; 1/2/2022 SUN. 6:00 AM - FINISH CLEAN UP CYCLE. TOOH & LAY DOWN 4.5'' DRILL PIPE, RACKED BACK 60 STDS 4.5'' IN DERRICK.; 1/3/2022 MON. 6:00 AM - FINISH LAYING DOWN DRILL PIPE & BHA.PULL WEAR BUSHING. RIG UP NABORS CRT & CSG EQ. MAKE UP SHOE TRACK, PUMP THROUGH SAME,RUN 5'',18#, P-110, WEDGE 513 CASING T/
12/27/2021 05 16431 9921 SCOUT CODE 5: 12/21/2021 TUES. 6:00 AM - DRILL 6 3/4" LATERAL F/ 16,540' T/ 17,518'.; 12/22/2021 WED. 6:00 AM - DRILL 6 3/4" LATERAL F/ 17,518' T/ 18,023'.; 12/23/2021 THURS. 6:00 AM - DRILL 6 3/4" LATERAL F/ 18,023' T/ 18,038'. BKREAM & TOOH TO BHA MM PARTED @ CONNECTION ABOVE BEND LEAVING 8.53' OF FISH IN HOLE. PULL WEAR BUSHING & TEST BOP'S; 12/24/2021 FRI. 6:00 AM - INSTALL WEAR BUSHING PU SIDETRACK ASSY/ RECEIVED VERBAL APPROVAL F/SIDETRACK 10:30HRS, 12/23/21. TIH W/ SIDETRACK ASSY AND TROUGH F/ 16,374' T/ 16,404'; 12/25/2021 SAT. 6:00 AM - TROUGH F/ 16,374' T/ 16,404'. UNABLE TO HOLD 165°R TOOLFACE.TOOH T/ 4,650'; 12/26/2021 SUN. 6:00 AM - TOOH LAY DOWN BHA PU NEW SIDETRACK ASSY W/ SECURITY FX73 BIT & 2°BEND MM. TIH T/ 16,374' AND 4% LUBE TO MUD SYSTEM. TROUGH F/ 16,374' T/ 16,604' @ 165° TF; 12/27/2021 MON. 6:00 AM - TROUGH F/ 16,374' T/ 16,604' @ 165° TF. TIME DRILL AS PER PLAN F/ 16,604' T/ 16,431'
12/20/2021 05 16540 9921 SCOUT CODE 5: 12/14/2021 TUES. 6:00 AM - FINISH TIH W/ LATERAL ASSY, DRILL T/ 11,117'; 12/15/2021 WED. 6:00 AM - DRILL 6 3/4" LATERAL F/ 11,117' T/ 12,816'; 12/16/2021 THURS. 6:00 AM - DRILL 6 3/4" LATERAL F/ 12,816' T/ 13,884'; 12/17/2021 FRI. 6:00 AM - DRILL 6 3/4" LATERAL F/ 13,884' T/ 13,940'. MM FAILURE, CBU, TOOH, LD BHA. PU BAKER RTTS PACKER, TIH T/ 9,648' ( 25' ABOVE FLT COLLAR). SET PKR AND TEST CSG T/ 1600 PSI FOR 1/2 HR; 12/18/2021 SAT. 6:00 AM - TOOH LD RTTS, FUNCTIONED BOP'S, PICK UP NEW LATERAL ASSY, TIH, DRILL 6 3/4" LATERAL F/ 13,940' T/ 14,127'. HELD BOP DRILL. 53SECONDS.; 12/19/2021 SUN. 6:00 AM - DRILL 6 3/4" LATERAL F/ 14,127' T/ 15,455'.; 12/20/2021 MON. 6:00 AM - DRILL 6 3/4" LATERAL F/ 15,455' T/ 16,540'.
12/14/2021 05 11323 SCOUT CODE 5: 12/8/2021 TUES. 6:00 AM - L/D 5" DP @ INT. CASING POINT ; 12/9/2021 WED. 6:00 AM - LAYING DOWN CASING TO REGAIN RETURNS ; 12/10/2021 THURS. 6:00 AM - CEMENT CASING, C/O PIPE RAMS ; 12/11/2021 FRI. 6:00 AM - TEST BOPS, PICK UP CURVE BHA AND 4.5" DP, TOOH FOR PLUGGED STRING ; 12/12/2021 SAT. 6:00 AM - DRILLING 6 3/4" CURVE ; 12/13/2021 SUN. 6:00 AM - TOOH TO PICK UP LATERAL ASSY. ; 12/14/2021 MON. 6:00 AM - TIH HOLE WITH LATERAL ASSY.
12/06/2021 05 9147 SCOUT CODE 5: 11/30/2021 TUES. 6:00 AM - MOVE IN RIG UP ON LABOKAY PAD; 12/1/2021 WED. 6:00 AM - RIG UP ON WELL. NU DIVERTOR. RU CELLAR PUMPS. PICK UP SURFACE BHA.; 12/2/2021 THURS. 6:00 AM - SPUD WELL 06:30HRS. 12/1/21.DRILL F/ 125' T/ 1849'. WIPER TRIP TO 1147' AND BACK TO BOTTOM. TOOH & LD BHA.; 12/3/2021 FRI. 6:00 AM - RU NABORS CSG CREW & CRT, RUN 10 3/4" CSG T/1051', CBU, RUN CSG AND LAND HANGER IN LANDING RING WITH SHOE @ 1839'. CIRC 1.5 CSG VOLUMES. CMT AS PER PLAN, TEST CSG TO 1500 PSI 1/2HR. RD CEMENTERS, ND DIVERTOR, NU CACTUS MBU WH & TEST T/3K. NU BOP'S & RELATED EQ.; 12/4/2021 SAT. 6:00 AM - FINISH TESTING BOP'S,PU 9 7/8" INTERMEDIATE ASSY. DRILL CMT, SHOE TRACK & 10' NEW HOLE TO 1859'.CBU, FIT TO 11.5# EMW WITH 220PSI. DRILL F/1859' T/2866'; 12/5/2021 SUN. 6:00 AM - DRILL 9 7/8" INTERMEDIATE F/ 2866' T/ 7120'; 12/6/2021 MON. 6:00 AM - DRILL 9 7/8" INTERMEDIATE F/ 7120' T/ 9,147, CBU IN PREPARATION TO TOOH
11/12/2021 01 20318 220' FSL & 2572' FWL OF SEC 20-T3N-R11W. PBHL: 100' FNL & 2317' FWL OF SEC 17-T3N-R11W.

PERFORATIONS

SERIAL NUM COMPLETION DATE UPPER PERF LOWER PERF SANDS RESERVOIR

WELL TESTS

RPT TYP TEST DATE RPT DATE OIL POT COND GAS DEL WATER BSW% FLOW PRES SHUTIN PRES CHOKE UPPER PERF LOWER PERF BOT HOLE PRES

WELL ALLOWABLES

EFFECTIVE DATE END DATE LUW CODE LUW TYPE CODE ALLOWABLE ESTIMATED POTENTIAL CURRENT ALLOWABLE TYPE

LEASE\UNIT\WELL ASSOCIATION HISTORY

EFFECTIVE DATE END DATE LUW CODE LUW TYPE LUW NAME REPORTING PCT PRIMARY LUW FLAG

LEASE\UNIT\WELL PRODUCTION

RPT DATE LUW CODE STORAGE FAC DOC USE WELL CNT OPENING STK OIL PROD(BBL) GAS PROD(MCF) DISPOSITION CLOSING STK PARISH

CASING

COMPLETION DATE CASING SIZE WELLBORE SIZE CASING WEIGHT UPPER SET DEPTH LOWER SET DEPTH CEMENT SACKS TEST PRESSURE HOURS UNDER PRESSURE TEST DATE CASING PULLED CREATION PROCESS

PLUG AND ABANDON

P and A DATE LOCATION TYPE CASING CUT TYPE CASING CUT DEPTH MUD WEIGHT LEFT COMMENTS

PLUGS

PLUG TYPE UPPER PLUG DEPTH LOWER PLUG DEPTH SACKS OF CEMENT SLURRY WEIGHT

TUBING AND PACKERS

COMPLETION DATE TUBING SIZE TUBING LOWER DEPTH TUBING UPPER DEPTH PACKER DEPTH

WORK PERMITS

REFERENCE NUMBER APPLICATION DATE EXPIRATION DATE WORK PERMIT TYPE WORK PERMIT STATUS WORK PERMIT STATUS_DATE TOTAL DEPTH WORK_PERFORMED DOCUMENTATION RECEIPT DATE TEST SAND WORK DESCRIPTION
20-22-6 01/18/2022 01/14/2023 SIDETRACK APPROVED 01/18/2022 0 N SIDE TRACK DATE- 12/26/2021, 1.5 HOURS. ORIENT TF TO 165 R A D TROUGH F/16.374 T/16, 04. TIME DRIL F/16, 404 T/16,431' AND
21-22-3-14 01/18/2022 01/10/2023 HYDRAULIC FRACTURE STIMULATION APPROVED 01/18/2022 0 N ZFRAC AND PERF AUSTIN CHALKK FROM 10,337-20,081. 39 STAGES.

Yep, the rig has drilled and cased the well.  Likely long gone by now.  The well is now approved for the frac and waiting on a completion crew.

Building on Skip's comment......

Operator had a heck of time getting this well / lateral drilled to TD based on the reports posted on SONRIS.

They were drilling lateral with no problems until twisting off drilling assembly at 18,038'.

  • Could not recover the fish (8' of section including drill bit) and had to sidetrack the hole.

Pulled back to about 16,400' to start the sidetrack and were successful in starting a new hole / lateral - drilled lateral to 19,100' and set casing.

  • Looks like lateral length is less than the planned lateral as per permit (10,300') - won't know until directional survey is posted but probably only about 8800-9000' of lateral drilled.

Sidetrack / new part of the hole is 49' from the original hole that contains the fish.

Questions / Concerns as to completion -

  • One has to wonder how the dogleg in this well associated with the sidetrack start point will impact frac operations. The more tortuosity of the lateral, there harder it is to effectively frac.
  • Other concern in the fact that this is about 1600' of open abandoned lateral less than 50' from the cased lateral. One has to wonder how this "void space" will impact frac stages started coincident with the new part of the lateral (e.g., frac gets into this void zone and deteriorates as to its potential stimulation impact).

PS - and totally unrelated comment - maybe I should offer classes in SONRIS report interpretation? LOL 

I'd go to class for sure.  :-)

Thanks Skip and Rock Man for explaining the well report in layman's terms.  I did note the 49' issue but thought that was in reference to the nearby well drilled decades ago. Very interesting insight to the drilling process, their complications and plan B sidetrack. I could never have deciphered that from the report.  Good point with your concern about fracking so close to the open lateral. We'll see what the future brings. Thanks again Professor!  

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